To address the control accuracy of large fuel flowrate during pressure fluctuation,a novel electro-hydraulic fuel metering unit(FMU)is constructed for afterburner fuel system of military aeroengine.Different from the previous FMU,the proposed FMU can achieve the higher precision opening control by a new metering valve with double control chambers(MVDCC),and realize the lower pressure difference fluctuation regulating by a novel two-stage constant pressure difference compensated valve(CPDCV)with dynamic damping orifice and damping piston.The experimental and AMESim simulation results verify the validity and superiority of the novel FMU.Since the temperature-induced variation in fuel properties and device capabilities may degrade or even impair the properties of novel FMU,the discharge flowrate is analyzed by global sensitivity analysis to research the effect proportion of each factor,the temperature effect is explored to ensure the working reliability in long-span temperature variation.Finally,the optimization of structure parameters for novel CPDCV can further reduce pressure difference fluctuation during pressure regulation,and the overshoot,adjust time and the integral of time multiplied by absolute value of error(ITAE)can be reduced by 24%,30%and 26%,respectively.This paper provides a reference for improving the stability of large flowrate during pressure fluctuation.
Current researches mainly focus on the investigations of the valve plate utilizing pressure relief grooves. However,air?release and cavitation can occur near the grooves. The valve plate utilizing damping holes show excellent perfor?mance in avoiding air?release and cavitation. This study aims to reduce the noise emitted from an axial piston pump using a novel valve plate utilizing damping holes. A dynamic pump model is developed,in which the fluid properties are carefully modeled to capture the phenomena of air release and cavitation. The causes of di erent noise sources are investigated using the model. A comprehensive parametric analysis is conducted to enhance the understanding of the e ects of the valve plate parameters on the noise sources. A multi?objective genetic algorithm optimization method is proposed to optimize the parameters of valve plate. The amplitudes of the swash plate moment and flow rates in the inlet and outlet ports are defined as the objective functions. The pressure overshoot and undershoot in the piston chamber are limited by properly constraining the highest and lowest pressure values. A comparison of the various noise sources between the original and optimized designs over a wide range of pressure levels shows that the noise sources are reduced at high pressures. The results of the sound pressure level measurements show that the optimized valve plate reduces the noise level by 1.6 d B(A) at the rated working condition. The proposed method is e ective in reducing the noise of axial piston pumps and contributes to the development of quieter axial piston machines.
A novel performance model of losses of pump was presented,which allows an explicit insight into the losses of various friction pairs of pump.The aim is to clarify that to what extent the hydro-mechanical losses affect efficiency,and to further gain an insight into the variation and distribution characteristics of hydro-mechanical losses over wide operating ranges.A good agreement is found in the comparisons between simulation and experimental results.At rated speed,the hydro-mechanical losses take a proportion ranging from 87% to 89% and from 68% to 97%,respectively,of the total power losses of pump working under 5 MPa pressure conditions,and 13% of full displacement conditions.Furthermore,within the variation of speed ranging from 48% to 100% of rated speed,and pressure ranging from 14% to 100% of rated pressure,the main sources of hydro-mechanical losses change to slipper swash plate pair and valve plate cylinder pair at low displacement conditions,from the piston cylinder pair and slipper swash plate pair at full displacement conditions.Besides,the hydro-mechanical losses in ball guide retainer pair are found to be almost independent of pressure.The derived conclusions clarify the main orientations of efforts to improve the efficiency performance of pump,and the proposed model can service for the design of pump with higher efficiency performance.